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Experimental Study of Flow Separation Control on an Airfoil by Suction and Injection

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dc.contributor.advisor Mashud, Prof. Dr. Mohammad
dc.contributor.author Hossain, Md. Farhad
dc.date.accessioned 2018-08-28T11:16:38Z
dc.date.available 2018-08-28T11:16:38Z
dc.date.copyright 2010
dc.date.issued 2010-05
dc.identifier.other ID 0805552
dc.identifier.uri http://hdl.handle.net/20.500.12228/414
dc.description This thesis is submitted to the Department of Mechanical Engineering, Khulna University of Engineering & Technology in partial fulfillment of the requirements for the degree of Master of Science in Mechanical Engineering, May 2010. en_US
dc.description Cataloged from PDF Version of Thesis.
dc.description Includes bibliographical references (pages 57-59).
dc.description.abstract In this research a new concept of flow separation control mechanism has been introduced to improve the aerodynamic characteristics of an airfoil. Control of flow separation over an airfoil which experiences a laminar separation bubble for a low Reynolds number is experimentally simulated under the effects of suction and injection. The suction and injection control mechanism appears to be suppression of the separation bubble and reduction of the upper surface pressure to increase the lift and decrease the drag. To perform the experiment of NACA 2415 airfoil profile has been chosen to make wing model. The wing model with control mechanism has been tested in a sub-sonic wind tunnel. The experiments are performed with different angle of aUack and different suction-injection frequency. The experimental results show that the flow separation control is possible by the proposed mechanism and benefits can be achieved by suction and injection. The wing performance is significantly improved due to control of flow separation by suction and injection. It has also been found that the lift increases about 14% and drag reduces about 23% at the angle of attack 8 degree. en_US
dc.description.statementofresponsibility Md. Farhad Hossain
dc.format.extent 71 pages
dc.language.iso en_US en_US
dc.publisher Khulna University of Engineering & Technology (KUET), Khulna, Bangladesh. en_US
dc.rights Khulna University of Engineering & Technology (KUET) thesis/dissertation/internship reports are protected by copyright. They may be viewed from this source for any purpose, but reproduction or distribution in any format is prohibited without written permission.
dc.subject Flow Separation Control en_US
dc.subject Airfoil en_US
dc.subject Suction-Injection Frequency en_US
dc.title Experimental Study of Flow Separation Control on an Airfoil by Suction and Injection en_US
dc.type Thesis en_US
dc.description.degree Master of Science in Mechanical Engineering
dc.contributor.department Department of Mechanical Engineering


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